The Proceedings of the Fluids engineering conference
Online ISSN : 2424-2896
2013
Conference information
0404 Investigation of the influence of unsteady flow field and purge air on the aerodynamic performance of a single turbine stage
Ken-ichi FUNAZAKIMamoru KIKUCHIShinya CHIDAKoki KUDOUAyumi MAMADAAkira TAKAHASHI
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CONFERENCE PROCEEDINGS FREE ACCESS

Pages _0404-01_-_0404-04_

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Abstract
This paper presents experimental and numerical simulation study of single turbine stage flow field with injected purge air. To investigate the influence of the purge air from the Rim-seal cavity, we conducted 5-Hole probe and Slant-type hot wire probe traverse measurement downstream of the rotor blade. Those measurement results were used to validate the numerical simulation data then we described the flow field of the rotor passage and cavity domain. In the case of injected purge air, Rim-seal cavity flow field tend to non-uniform and we observed unsteady vorticity distribution around cavity outlet. Those flow filed entrained streamwise vorticity and entropy generation rate in the rotor passage.
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© 2013 The Japan Society of Mechanical Engineers
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