2021 Volume 29 Issue 1 Pages 29-34
In order to improve the thrust performance of ion thrusters with pulse width modulation control, optimized grid system by numerical simulation was used for the reduction of leak ion beam current. The effect of reduction of mass flow rate on thrust performance was also investigated for the improvement of propellant utilization. The leak current was decreased from 30% to 3.5%, achieving dramatic improvements. The propellant utilization was also improved from 0.25 to 0.48 by decreasing the xenon mass flow rate from 9.8 ug/s(0.1 sccm) to 4.9 ug/s(0.05 sccm).