石油技術協会誌
Online ISSN : 1881-4131
Print ISSN : 0370-9868
ISSN-L : 0370-9868
講演
坑井能力改善に向けてのデータ取得, 活用例
(勇払圧入井のケース)
泉 胤智細越 公氏若林 尚幸
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2010 年 75 巻 6 号 p. 428-435

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Japex has been operating Yufutsu Oil & Gas filed in Tomakomai, Hokkaido. The new water injection well drilled in 2009 has very good reservoir characteristics and productivity is also very good, but injectivity declines rapidly with increasing the cumulative volume of injected water.
We took many wellbore data concerning pressure and temperature, and tried to consider the cause of the damage. With an analysis of the data, we considered that the damage is due to the mud cake stayed between the 5″ Slot Liner Casing and 6″ wellbore. We tried to remove the mud cake by Pulsonix cleaning and Acidizing treatment, and succeeded to recover the performance by eliminating most of the foreign object.

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