構造工学論文集 A
Online ISSN : 1881-820X
コンクリート構造・橋:論文
過剰たわみが生じた東名高速道路跨道橋の原因推定と安全性評価
吉野 通範菊地 新平若月 健司千々和 伸浩
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2023 年 69A 巻 p. 734-741

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The overpass of the Tomei Expressway has been in operation for 50 years, and repairs are progressing with aging. While the overpass in Fuji City, Shizuoka Prefecture, has also been inspected and repaired, many cracks have been detected on the lower surface of the PC-girder of the standard oblique π-shape bridge and the decrease in prestress is suspected as a cause. This paper reports the results of investigations to estimate the cause of the measured deflection and assess the structural safety of the bridge.

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© 2023 公益社団法人 土木学会
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