TRANSACTIONS OF THE JAPAN SOCIETY FOR AERONAUTICAL AND SPACE SCIENCES
Online ISSN : 2189-4205
Print ISSN : 0549-3811
ISSN-L : 0549-3811
Experimental Validation of Off-design Combustion for Liquid-propellant Rocket Engine High-frequency Instability
Takeshi KANDAShunsuke KIKUCHIHonoka KINO
Author information
JOURNAL OPEN ACCESS

2021 Volume 64 Issue 1 Pages 13-21

Details
Abstract

The mechanism causing high-frequency combustion instability was presumed to be the progression of combustion at an off-design location; that is, in the vicinity of the faceplate. Experiments were carried out to prove this. In the experiments, water was used to simulate the propellant and the increase in pressure caused by off-design combustion was simulated by injecting nitrogen gas. Pressure increase and decay were measured to within approximately 1 ms, and the maximum local pressure was approximately twice the pressure prior to increasing the pressure. To estimate the pressure change in actual engines, a simplified simulation calculation model was constructed. After calibration using the experimental results, the time and amplitude of pressure change were on the same order of magnitude of those of the engines. The present study results show that the off-design combustion model can be a cause of the high-frequency combustion instability experienced when using liquid rocket engines.

Content from these authors
© 2021 The Japan Society for Aeronautical and Space Sciences
Previous article Next article
feedback
Top