土木学会論文集B1(水工学)
Online ISSN : 2185-467X
ISSN-L : 2185-467X
水工学論文集第57巻
手取川の洪水時の礫河原再生工の変形要因の検討
前野 詩朗忰熊 公子吉田 圭介山村 明
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2013 年 69 巻 4 号 p. I_721-I_726

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After the Dainichigawa dam construction gravel supply to downstream from the dam site decreased in the Tedori River. As a result, river bed degradation progressed and gravel bed area gradually decreased. Furthermore, exposure of soft rock remarkably progressed around 14km to 15km from the river mouth. The exposure of soft rock not only endangers hydraulic structures but also deteriorates river environment. Therefore, gravel bed restoration works using groin group composed of connected stones were carried out. After the groins installation, parts of the groin were deformed during the flood in 2011. This paper aims to clarify the deformation mechanism of them using two-dimensional flow analysis. Numerical results showed that the hydrodynamic force acting on the groin caused by high velocity surpassing its design transformed the parts of the groin.
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© 2013 公益社団法人 土木学会
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