河川技術論文集
Online ISSN : 2436-6714
堤防被災箇所における変状機構解明事例からの考察
植野 直美檀上 裕司小俣 雅志長谷川 浩夫水草 浩一西尾 仁志
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2008 年 14 巻 p. 75-78

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During the torrential rain on July 2006, the water level exceeded the design water level at the Nadabun station along Hii River. The trench excavation investigation was conducted at Imazaike, which is one of two places where the cave-in on the downstream surface and the leakage in the channel at the toe of dike were identified. The things carried out were the geotechnical investigations, the in-situ tests at the excavation site, and the water quality analyses. It is shown that the cave-in on the downstream surface should be due to a cavity caused by the piping and outflow of sand in the foundation ground below the dike body. It is considered that the main reason for the cave-in is the rising phreatic surface by spring water and seepage block caused by the existing dike-toe channel.

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© 2008 土木学会
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